Continued

 

 

Another area of concern for Major Fitzwater was a JP-4 fuel shortage. Instead of the 35,000 gallons that was supposed to have been reserved for the test aircraft, on December 29 the Navy was asking if 11,000 gallons would be enough until a tanker ship arrived on January 6. Using a rule of thumb of 1000 gallons consumed per day, Fitzwater figured that-considering the possibility of weather-caused flight delays-he probably could get by with that amount of fuel. However, if the weather turned out to be good, Slide III tests would have to be suspended. After a 1 hour and 30 minute flight on January 2,1961, the major was told that the test site fuel bladder was empty. An additional day of testing was completed using fuel already aboard the aircraft. For the testing on January 4, the aircraft was refueled by draining 5000 lbs. of JP-4 from the fuel line, which connected the test site fuel bladder to the base tank farm several miles away.

 

As part of the Flight Plan being followed by the crew, the next series of tests were to determine the side loads imposed on the C-130BL ski landing gear during turns when taxiing at high speeds. The plan called for the aircraft to turn in 400 ft. and 200 ft. circles at various speeds from 21 to 48 mph. The test target was to obtain an accelerometer side-load reading of 0.5-g during the turns. That objective could not be met, however, since the aircraft skidded sideways in the area's soft, dry and powdery snow at any higher than 0.2-g readings.

 

During one taxi turn test on January 5 the nose ski, being deflected in the turn, directed a steady stream of snow into the No-3 propeller and engine air intake causing a flameout. The test was terminated when it was observed that the blade angles were unsymmetrical on the four propeller blades. After taxiing back to the parking area, it was further observed that the prop blades had been rotated to positions that exceeded the limits of the pitch control gears. Since repairs were not practical in the field, a replacement propeller and tools were requested to be sent from Christchurch. Nine days were required to air transport the replacement prop from New Zealand because of delays caused by high en route winds.

 

The replacement prop arrived via C-130 from Christchurch on Sunday, January 15. The old prop was removed and the new prop was installed by 1800 hours. An engine run verified that the new prop was OK-but the engine was not. A visual inspection revealed that the engine's main shaft had a permanent set of about 3-degrees. This damage required an engine replacement-which would have to be done at Christchurch. The aircraft departed Williams Field on January 17 and the engine change was accomplished by the 22nd. While at Christchurch, Fitzwater had some repairs made to the test instrumentation installed on the skis, which had suffered some damage from ice. Because of the instrumentation repairs and poor weather conditions, Fitzwater and crew were unable to return to McMurdo until February 6. Test flights resumed the next day.

Because of the time lost due to the repairs and weather, it was decided to eliminate three items on the Test Plan for tests at intermediate gross weights and instead proceed to tests at the full 135,000 lbs. gross weight. It was also decided to delete the tests scheduled to be performed at Byrd Station and South Pole Station as called for in the Test Plan. The primary concern was that the remaining tests be completed before the mandatory cutoff date for the program, which had been established as February 15. That date was based on the availability of transportation back to the U.S. for personnel of the Task Force and to make room at McMurdo for an influx of personnel from outlying sites. Task Force Slide III flew right down to the wire, making the last test flight on February 14, 1961. From February 9 to the 14th, Fitzwater had made 19 ski takeoffs and landings at 135,000 lbs., including one takeoff employing RATO bottles.

 

 

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